TheAnesthetist
Well-Known Member
- TheAnesthetist Well-Known Member
Yeah that's for 1000 miles per year. The next step up is 3,000Was there a mileage limit?
Yeah that's for 1000 miles per year. The next step up is 3,000Was there a mileage limit?
I remember cleaning the rust/gunk off the damper and it actuated smoothly. I believe the diaphragm is intact as I had it off and was able to hold suction with my thumb plugging a hole.Check your bypass hoses and valve to ensure that builds boost at high throttle.
What did you do to bypass it and what are there any repercussions? I have a 2.8” pulley and don’t want to blow the darn thing upI can’t find a photo on my phone of the bypassed unit by will get a photo later when I get home.
My blower is loud, it makes noise at -5psi. It’s even louder after plugging the noise reduction holes. Those photos are on my computer…..
Valve and shaft move easily between closed and open. I can close it by pushing on it with my finger. I will try to find time this weekend to take a drive and pay attention to the boost gauge and get a GoPro pointed at the shaft to see if it is actuating.Here is some pics of manually testing if the bypass valve moves correctly. You can put a camera on it, and see if it moves the full range.
How the boost bypass works. My explanation of the boost bypass.





I’ll bypass the solenoid and see what happens, thanks for the pictures and explanations by the way.The kid I bought my donor from told me something on the SC setup failed so he did the bypass. My bypass actually hold pressure when testing out of both ports. So, I’m guessing it’s the solenoid that messed up and he did this routing to ‘fix’ it. Give it a try just to make sure your making boost.
Referencing the electronic boost gauge I was around 3-5psi normal and after the bypass went to around 14ish? I was caught off guard as I have never experienced it under more boost before haha. It definitely did the trick. I will be ordering another solenoid to see if it fixes the issue.The kid I bought my donor from told me something on the SC setup failed so he did the bypass. My bypass actually hold pressure when testing out of both ports. So, I’m guessing it’s the solenoid that messed up and he did this routing to ‘fix’ it. Give it a try just to make sure your making boost.
I’ll have to see if I threw my dimmer switch out, I may have to get into that connector and see what it does with the wires unhooked. I would think with the headlights turned on and wires soldered together it should be a lot brighter than it is. When I turn the auto headlights off it is an incredible difference in brightness. You can read it very clear in the daytime.I kept the factory dimmer cause my eyes don’t like excessive ambient light after driving for a while. I’d have to look at the schematics to see what dims the IPC but I’d believe it would be in the bcm